| Interior
Trim Removal |
| The interior
trim was in pretty bad shape, moldy and stained. When I
tried to clean them nothing worked. I tried bleach,
softscrub, acetone, sandpaper. The mildew goes deep into
the vinyl. I don't have plans for replacing them yet. I
may try to find a substitue. |
 |
Mildew stains, impossible to remove
even with tolulene
|
| |
| The trim just
peels off. It is harder to put back though because the
vinyl is not as pliable as it once was. |
 |
Comes off pretty easily
|
| |
| After removal I
could see dirt and stains where the portlights had been
leaking. |
 |
Dirt and stains at bottom of
portlight due to leaking
|
| Frame
Removal |
| After removing
the screws I used a putty knife to cut the caulk all
around the edge of the frame. Once that is done you can
gently pry off the frame being careful not to bend it. I
marked each frame as I removed them port or starboard,
forward, mid or aft and top. I do not want to drill new
holes so this will allow me to put them back in the same
orientation. |
 |
Putty knife all around to cut caulk
|
| |
| Once the frames
were removed I could see places where there were leaks.
The wood was dark in some spots but still solid. In some
cases there was no wood but it looked like that's where
the plywood ended and not due to rot. It was a major job
to remove the old caulk. I tried everything including the
special stuff for removing caulk. The best way I came up
with was to use a razor to get most of the stuff, then
use Goo Gone and a plastic stick to rub the thin layer
off. It was a lot of work but it came out clean. |
 |
Some leakage apparent but wood
still solid
|
| |
| This shows new
looking wood. Not bad for a 25 year old boat. |
 |
Solid wood, no leaks
|
| |
| Once the frame
was removed I could see where there as little to no caulk
and dirt had seeped in. Almost every portlight showed
signs of leaking especially in the corners. |
 |
Dirt shows where caulk failed
|
| |
| I noticed some
separation between the cabin liner, the deck and the
plywood. I will epoxy these back together but I don't
think it's structurally serious (at least I hope). |
 |
Cabin liner separated from wood,
not serious
|
| |
| Short measure
here on the plywood! |
 |
Wood gone or never there? Will fill
with epoxy.
|
| |
| It also looks
like there were some filled in screw holes so I may not
be the first one blazing this territory. |
 |
Old screw hole means others have
travelled this path before me.
|
| |
| All done with
removal. Kind of scary leaving those big holes there for
the winter! Hopefully the tarp will hold. |
 |
Portlights removed for winter
restoration
|
| Frame
Installation Prep |
| OK, fast forward
to spring. Here the openning is being epoxied back
together. I used filler for spaces where the wood was
missing. |
 |
Close up view
|
| |
| Lots of clamps
are necessary to ensure a good bond. I feel better
knowing that the area around the portlights is solid. |
 |
Epoxy and clamp to repair
separations
|
| Frame
Restoration |
| Back to winter
and the inside work. When I first got the boat the
portlights leaked very badly. As a quick fix I put a coat
of silicon caulk over the spline. This slowed the leaking
down considerably so I could launch the boat and sail.
Unfortunately, the caulk was very hard to remove from the
frame. Oh well, such a small price to pay for a longer
sailing season. |
 |
I put silicon caulk over the
splines to help reduce the leaking.
|
| |
| Flipping the
window over it is apparent why the corners leaked so
much. Due to the curvature of the frame the space between
the window and the frame gets larger so that the foam
tape does not close it. This leaves a gap that is only as
watertight as the spline. When the spline gets old and
cracked it is no longer watertight so there will be leaks
where the foam tape is not a good seal. |
 |
Before window removal, old foam
tape has gap where leaks could occur
|
| |
| To remove, the
handy-dandy putty knife comes in handy. Just slide it all
around to break the seal. |
 |
Removing the spline
|
| |
| I could not tell
where the seam was so I just picked a random spot and
pried away. Care was taken to not scratch the frame.
They're pretty banged up anyway but no need to put new
scratched in. |
 |
Hard to get started but comes out
easy.
|
| |
| Peel away! OK, I
took a lot of pictures so I could show every step.
They're just little digital bits that don't take up much
room anyway. |
 |
Out with the old
|
| |
| This is
exciting, like an archaelogical dig. It is very clear
where all the leaks were. |
 |
Really bad leak here
|
| |
| I wonder if this
was the original 1980 spline? |
 |
Old spine badly deteriorated
|
| |
| Oh, the back
side. |
 |
Back side of spline
|
| |
| Here is another
problem, the window is not a very tight fit to the frame
so there is not much tape holding it on. |
 |
Poor fitting window has marginal
seal
|
| |
| Wow, UV and salt
air took its toll on the spline. The new one should
provide a much better seal. |
 |
Cross section of old vs. new spline
|
| |
| The foam tape
was pretty easy to remove but the glue left behind was
not. A little Goo Gone (what's in that stuff anyway?) and
some rubbing got rid of the glue. The silicone caulk was
not as easy to remove but lots of elbow grease latter and
the frames were looking good. |
 |
Remove old foam tape with razor
|
| |
| I don't know why
this gap is not welded over like the other parts are. Any
water that got past the spline could get in through this
gap and suspect that was where most of the water was
coming from based on the gunk found around the gap. |
 |
Gap in frame also source of leaks
|
| Portlight
Reconstruction |
| I decided to get
new windows because the old ones were hard to clean and
they were scratched. I cut some templates for the glass
place and they ordered a piece of plexi for me. When I
got them back home one of the windows was a different
tint (I suspected something might be wrong when only one
had a different backing paper.) Back to the shop where
they cut 6 new ones from a piece of Lexan. The Lexan
seems stiffer but not by much. I don't think it is any
more resistant to scratches either. I plan on taking VERY
good care of them after all this work is done. |
 |
Opps, the glass place screwed up.
Two different tints!
|
| |
| I got the foam
tape from the Tanzer Parts place (see the association
website). Their instructions is to put the sticky side to
the window. I didn't like that idea because it would be
hard to line up with the frame. You would have little
bits of foam tape sticking out. I decided to put the
sticky side to the frame like the original installation. |
 |
New foam tape, sticky side toward
frame
|
| |
| In the original
design of this portlight the water tightness comes from
having a seal between the spline and the window, between
the window and the foam tape, and between the foam tape
and the frame. This was just too many opportunities for
failure. I decided to add some caulk between the window
and the frame so that there is at least one tight seal. |
 |
The good stuff, just don't drink
it.
|
| |
| Here I show the
foam tape in place with a thin bead of caulk placed in
the corner between the tape and the frame. |
 |
Thin bead of caulk to form
window-caulk-frame seal.
|
| |
| When the window
is put in place it forms a nice seal to the frame. The
extra adhesion to the window is good too. |
 |
Window in place, nice seal to
frame.
|
| |
| I thought this
step would be easy but it was a real PITA!!! The new
spline was thicker so it was hard to squeeze in. The
frame had been bent in a few places which made it even
harder. I tried using some kind of tool to help push it
in but I didn't want to damage the spline. Fingers worked
the best but they got very sore. It is also very
important to push as you squeeze so the spline does not
stretch and slide out when you're done. |
 |
Insert new spline, pushing in and
back as you go.
|
| |
| The section
where the weld was made it difficult (what do you expect?
Easier?) to push the spline in. I ended up trimming a bit
of the spline to get it in. |
 |
Trim a little to get around weld
area.
|
| |
| OK, that was WAY
too much work to do. I can't believe I've got 5 more to
go! |
 |
A completed portlight! One down,
five to go.
|
| |
| What a feeling
to get this part of the project done. |
 |
All done! That was quick (not!)
|
| Portlight
Installation |
| Spring is here!
Time to put the boat back together. I hope I have all the
pieces. I used lots of caulk because it is better to
have too much than too little. You know what they say,
"Caulk is cheap". Ouch, that hurt.
|
 |
Lots of caulk this time! (Caulk is
cheap)
|
| |
| Before putting
the frames back on I dabbed caulk into the little gaps.
Careful not to put too much here because if I ever put
the interior trim back on this will get in the way. |
 |
Caulk frame gap too
|
| |
| I used all new
#6 SS screws because the old ones had too much caulk on
them and some were stripped. I tightened them down snug
but not tight. The caulk needs to have some thickness for
a good seal. |
 |
Completed portlight, you can see
through it!
|
| |
| I decided not to
wipe the caulk off because I was afraid of it sticking to
the anodized frame. Not sure if that was a mistake but it
was pretty easy trimming off the cured caulk with a
razor. |
 |
Very nice ouzing
|
| |
| DONE, DONE,
DONE!!! |
 |
Looks much nicer with good
portlights!
|